Tuesday, April 20, 2021

Spring Fling Cruise 2021

Cruising weekend to Lake Boca


Weather for the weekend was forecast to be ideal for an easy cruise up to Lake Boca, so we made plans to get out on the water - we were not alone!

Leaving the dock just after 12:30, we easily navigated down the New River, past the Swing Bridge, on to 7th Ave Bridge. The FEC Railroad bridge was up but there was radio traffic that indicated at least two large tows were heading up river. We communicated with the skippers that we were ok waiting on the upriver side of Andrews Avenue Bridge. Both of the big tows past us holding in pretty slack water and a third big yacht joined the upstream crowd. Once they cleared Andrews bridge, we throttled up and passed Andrew's close to the North side fender. Third Avenue bridge was already aware that we were outbound, but etiquette demands that we call to request opening. They quickly opened the bridge so we really didn't need to hang around between Andrews and 3rd.

Once past 3rd avenue bridge, we joined a few other boats that were headed down the river. Sometimes, following other boats is more stressful, some of the smaller boats are not very well educated about navigation rules, so guessing what they might do is fraught with challenges.

As we continued on down the river, I worked at getting the boat's running rigging setup for sailing.
Starting at the Bow, I released the hold back line that prevents the furler from unrolling in heavy winds, we needed to be able to unfurl (deploy) the Genoa. Back to the Mast, I connected the Main halyard to the head of the main sail, making sure it was not twisted around any of the other lines that went to the top of the mast. Made sure that the reefing lines were free and not likely to get tangled when we hoist the main. Check that the Dinghy was secured to the deck and not likely to get pulled free in heavy winds. Not that we were expecting any strong winds, the forecast was for winds gusting to 14 knots. I took a few minutes to lower the Lazy Jack lines on the Stbd Side of the stack pack. Moving back to the cockpit, setup the genoa sheets on both the port and starboard winches. Head down to the cabin and get the Winchrite electric winch handle and secure it close to the Starboard winch.

After releasing the line clutches for the 4 reefing lines (two each for the 1st and second reefs) and releasing the boom securing line which prevents the boom from moving side to side when motoring or at the dock/anchor. Checking the outhaul tension, light winds, light tension. A quick test that the traveller car was free to move on the traveller. All set, we just need to be able to turn into wind before hoisting the main.

As we passed marker #5, we left the New river, turning out towards where it joins the Intracoastal waterway, we saw a lot of boats hanging out at the Sand Bar, which included several drink bars! It was a little surprising, this was Friday early afternoon. 

We continued out joining the other craft that were heading down the ICW towards the 17th street causeway bridge, most of them small stuff, a couple of boats that had to wait till the bridge raised in order that they could pass the open bridge. No cruise ships in site, but the Port police were out in their boats to ensure that nobody strayed into the Turning basin, we've done that before and know better now.

Once past the corner on our Port side, we turned out into the Port Everglades Channel. The channel was pretty calm and the waters looked peaceful. Of course, a few dozen fast power boats quickly churn up the waters and we, travelling at around 5 knots, get pushed around quite a bit. We've been out there in much worse conditions, to we took this in our stride. Motoring, we headed out to the PE1 buoy before briefly turning South, into wind, to raise the mainsail, no issues, the electric winch handle quickly hoisted it all the way up our 50 high mast. With the Stbd lazy jacks lowered, and with the wind just off of the port bow, the main raised without issue. 

With the Mainsail up, we turned North and unfurled the Genoa, 100% no need for reefing, the wind was light. We turned to the North East in order to reach the Three Mile limit - we needed to pump out and we never break the law. Once we passed over the 3 mile line on the GPS, I went down to the cabin, unlocked the dump thru hull, opened it and ran the Macerator, meanwhile, Peggy checked over the stern to let me know when the the tank was empty. Turning off the Macerator, closing the Thru Hull and relocking it, pump out was complete. We returned to our Northerly course. We were getting 2 knots push from the Gulf Stream. 

Sadly, the wind was dropping and our course had the wind over the stern, our speed dropped down to 3 knots, not a comfortable sail, downwind, slow and long! Looking at our GPS calculated arrival time at Hillsboro Inlet, I figured it was time to start up the engine and lower the sails then turn in directly to the inlet.

Despite it being close to low tide, we passed through the Hillsboro Inlet without seeing any depth less than 9 feet. Checking the Hillsboro Inlet Depth report we knew which course to follow. It pays to research before going in through any inlet.

After a short time holding for the Hillsboro Inlet bridge to open, we raised the engine RPM and got our speed up to 7 knots (this was not possible before our prop and shaft were treated with PropSpeed back in  January 2021). The stream was still pouring out of the Inlet, I increased the RPM to 2100 and we were just under 8 knots through the water, but we had over 3 knots against us, so we passed by the open bridge at just 5 knots. 

Once passed the bridge, we thanks the tender and turned to Starboard heading to Hillsboro Blvd Bridge. The Bridge opens on the hour and half hour, we passed the HI bridge on the hour that gave us 30  minutes to get to the Blvd bridge, even at our new higher speed, we would be really pushing it to make that bridge in 45 minutes and the next opening we could make would be on the hour. So we slowed down and took a very relaxed motor North. Time for lunch: Crackers, Guacamole and Potato Salad with a GZero drink, surprisingly good.

We timed arrival at the Hillsboro Blvd Bridge perfectly catching up with several boats that waked their way past us only to have to wait at the bridge. The bridge opening was delayed a few minutes, just enough to ensure we would not make the 20 minute trip up to the Camino Real Bridge, so we took it easy again, shooting for the 20 past bridge opening. 

As we passed Camino Real, we got our first glance of Lake Boca and it's popularity this weekend - CRAZY.

Most sailboats anchor in the North East Corner of Lake Boca where the depths are over seven feet, plenty deep enough for our keels. Anchoring spots were hard to find because there were so many boats on the lake, and, don't forget, it's FRIDAY afternoon!! We passed around the deeper channel around the lake and ended up anchoring on the East side of the lake half way between the North and South extremes. We were anchored just to the East of a Catalina 34 named 'Cheerios' which was owned by a club member just a few weeks ago, he sold it. In front of us was a Motor Yacht named Special K - Cheerios and Special K - We looked behind us and another motor yacht was at anchor astern of us, not behaving very politely, I guess we had Cheerios' to Port, Special K ahead of us and a bunch of Flakes behind us. 

Bada Bing Bada Boom

We could see a few other boats from the Hillsboro Inlet Sailing club on the lake, but we were ready for an early dinner and early bed. First we put the Dinghy in the water ready to use it in the morning when we would go visit.

With the Dink off of the boat, we were able to raise the hatch above the V-Berth and with the little wind we had, it was cool enough. In the Galley I prepared Meatloaf and Mashed Potatoes, followed by Klondike bars, washed down with a glass of Pinot Grigio for Peggy and a mile Red Blend for me.

Goodnight. Saturday deserves it's own post! See you on the water.






Thursday, April 15, 2021

Fresh Water Plumbing - Shut off valve

Shut off valve for the Fresh Water Plumbing System

 


This is the modified Plumbing system that I did in April 2020, this past weekend I found a defect in the design.

After purchasing new water filters (set of 3) for a change out before our trip this past weekend, it only took a few minutes to remove the 3 filters. To do so, the whole house filter is accessed by removing the center draw from the galley undercounter and then the two filters for the drinking water system.

Then the phone rang and I needed to answer it. My buddy was calling to ask about our meet up later that day. It took a few minutes to deal with the call but I could hear water running, I figured that there was a small amount of water syphoning out of the whole house filter housing. After the call and as I prepared to put the new filter in place, I realized that the 'small amount' had filled the bilge to the point where the bilge pump was about to run!! The 3 way valve does not work, it does allow selection of either the Mid or Aft tanks, but it does not stop the flow in it's third position.

During those few minutes, the aft tank and mid tank drained about 15gallons! 

Solution is to add a shut off valve between the selector and the whole house filter.




Pex Shut-off Valve installed on the pipe
from the Tank Selector to the House Filter
Shown in the Shut position.


This project took 4 hours 10 minutes.
3 hours to find the pex tools - Duh, in the Garage in a box marked 'PEX'
1/2 Hour to drive down to the boat
10 Minutes to remove the Galley Drawers, Cut the pipe, Install the Shut off valve, Test it, Reinstall the Galley Drawers.
1/2 Hour drive home.

The dribble of water on the pipe below the shut-off valve is just from the filter when I cut the pipe. We had drained the tanks earlier this week, part of our water health routine.

We filled both water tanks, no leaks. 

It's easy to reach the shut-off valve when I need to remove the water system filters. Life is good.

See you on the water, we're heading up to Lake Boca on Friday, back on Monday.



Monday, March 29, 2021

Shout out to Prop-speed

Prop-Speed

Wow!



We had our boat's prop and shaft coated with Propspeed when we had Eximius out of the water in January. I mentioned, in a post at that time, how pleased we were with our boat's performance due to the prop-speed finish.

Since then we have had 3 weekend trips out, a couple up and down the ICW and one outside on the Ocean. All involved working our way up and down the New River in Fort Lauderdale.

Why 'Wow' ?

Because we had never seen 8 knots over the water before, never. We had gone just over 8 knots over the ground when we had a 3 knot gulf stream current carrying us along, but never over still water.

This weekend was a great example: We were coming in to Hillsboro Inlet close to low tide - I know, not the best time to come in through that bridge - well, at 2,000 rpm we were doing 7.6 knots through the water but only 4.4knots over the ground, which meant that we were going against a 3.2 knot current - BUT WE WERE DOING 7.6 KNOTS AT 2,000 RPM ! That's 'Wow' !!

On our return trip from Lake Boca, we were rushing to catch the bridge, but we had a 2 knot current against us, I pushed it, raised the rpm to 2,200 and we were doing 8.3knots, we were doing 6.3 knots over the ground- that's beyond 'WOW' !!

I contribute this wow to having our prop and shaft painted with Prop-Speed and the nice job Patagonia Services did on the boat's bottom.




So, a well deserved Shout out to Lehandro of Patagonia Services.

Thanks Guys!

See you on the water.
 


Sunday, March 28, 2021

Alternator tach failed

 Alternator Tachometer failed.


Our Alternator Tach failed on our trip out a couple of weekends ago. I guessed it was probably the wiring at the alternator. A quick look at the back of the alternator I could see that the white wire (tach) was broken. After removing the plug I also found the the sense wire (blue) was hanging on by a thread.

IMHO  - the wires from the Alternator plug are too short so the connections to those wires are subject to a lot of vibration strain.

We spent an entire afternoon searching local auto stores trying to find the standard auto part, eventually we found a store that had two. Looking at them both, one appeared to be defective, so I only purchased one. The wires are longer !!

It only took about 30 minutes to install the new plug and connect it to the engine harness. The new plug connector was $39.

With everything wired up, we did an engine check and all was fine. We're ready for our trip next weekend.

When I got home I did a search on Amazon for the connector. Most of the online auto supplies were the same cost. 

But this is for a Dorman 645-906 Blower Motor Resistor Pigtail $14.95 Same item!!!

Now I have a spare.


See you on the water.

Sunday afternoon and I could do with a Beer.

 Fixing the Head


This is our Jabsco Head Pump. We are very careful when it comes to taking care of our head system.

This pump is normally used to pump the poop out of the bowl and to flush the bowl with water, however, I disconnected the water supply to the pump (it was a salt water supply) and we keep a flushing jug in the bathroom. We've tried various jug sizes, turns out the best so far is a 2.44 quart OJ container, we fill it to the 2 qt mark and that helps us keep track of how much is in the tank.

Back to the Pum fix.

Peggy complained about the pump being too stiff last weekend we were out, and it really was. In the past a quick lube with teflon lubricant did the job. But this time there was black sealing rubber coming out of the top of the pump shaft (under the grey handle)


Time to pull it apart and fix it.

The top of the pump is secured in place with 6 screws. But why on earth do they still use Flat Head screws  on anything ??

But they do, so I carry the tools.















The flapper valves are getting old, and I carry a repair kit for the toilet on board.

It only took a few minutes to remove the whole valve assembly, clean up the surfaces beneath that and put the new flapper valve in place.

The big hole in this pic is where the pump does it's job. It looks cruddy but cleaned up with a few Chlorox Wipes got it done.

The big "O" ring on the end of the Pump shaft was next, two pairs of pliers quickly removed the nut on the end of the shaft, but then I found there's no need to remove the O-ring holder. There's a flat on the lower side of the holder that allows for easy removal and replacement of the O-ring.



Before putting everything back together, copious amounts of Teflon lube was slathered on the pump O-ring, and the seal where the pump shaft exits the top of the pump casing. That needs to be replaced, but the kit I had did not include that seal, time to get another kit - with that seal.

Works a charm now.

This is the wrong kit! Ours looks like the center of those 3.

Although the handle is Gray. And the boat was built in 1987, but perhaps the head is newer that that.

Another Sunny Sunday Afternoon, listening to the Beatles Fixing a Hole - how appropo!

Head's fixed. 

See you on the water!


New Bathroom Lighting Pt. 2

 New Bathroom Lighting

What do you do when at Anchor early and there's time to twiddle your thumbs?
Complete the install of the new lighting for the bathroom (head).

Very happy even though I only installed one of the White LED strips and one Red Strip.


The two switches are mounted on the bulkhead just inside the bathroom door with the wires running inside a heat shrink tube that is double sided tape glued to the bulkhead.

Just like in the galley lights, the switches are setup to be Red (Rear), white is the forward of the two switches.





The video shows the None - White - Red lighting.



Oh, and just in case you wondered when I type up my blog posts, Peggy snapped this while I was setting up this post.

It's about 5:45pm Sunday March 28th, 2021, On the boat at anchor at Sunrise Bay. My laptop is networked with my Phone's Hot Spot. Love my T-Mobile service.

The install was completed when we were on Lake Boca yesterday.

What else did I do this afternoon after we motored down the Intra Coastal Waterway from Lake Boca, Florida to Sunrise Bay Florida - I'll post that next - someone has to do it.





See you on the water.






Thursday, March 18, 2021

New Bathroom Lighting


Updating the lighting in the Bathroom (head)

I installed LED lights in the bathroom several years ago with some LED Puck lights

They were a lot better than the original Festoon lamp but I would not install them again. 

The light switch was located on the aft bulkhead of the bathroom where the original power cord passed from the other side of the bulkhead, that's the Port Side Cockpit locker.

After installing the Red and White Galley lamps in 2019, we both agreed that they would be better suited for the lighting in the bathroom and having the Red option would improve our night vision if we had to go.  Go - get it?

This past weekend, Peggy reminded me that we needed to change out the lights, a quick reorder on Amazon and the new lamps arrived this week.


These 12" LED strip lights will mount beneath the cabinets in the bathroom.

I purchased 2 packs, one Red the other White, each pack has 4 strips of lights.

I'll use two of the whites and two of the red strips with switches for each color.

I should be able to mount the switches close to the bathroom door or at least convenient to reach when entering.





The simple on/off switch has VHB tape on the back, so easily mounted, the challenge is to run the wire so that as little as possible is exposed, both aesthetically and so that the switch is out of the way when we take a shower.

I might even mount the switches outside of the bathroom.

The switches were available in various lengths of wire, I chose the longest, 78" that should be plenty.

Of course, I'll have to pull out all of the contents from the Port Side Cockpit locker in order to get to the original wiring.

I'll run new wiring back to the electrical panel which is another project that is getting closer and closer.



We might get this project underway this weekend, looks like a storm is heading our way and will leave our weeklong trip to Biscayne Bay in jeopardy, baby steps.

Part II of this post will be the actual installation. If we do get to go down to the Bay, then I guess the install will be while we are on the water.

So, see you on the Water.