Thursday, August 24, 2017

Time for the Kitchen Sink

I Know! It's a 'Galley' Sink

But that doesn't affect the fact that it frequently gets blocked and drips yuk onto the Cutlery tray in the draw beneath the dual sinks! So it's time to fix it.

The original drain fittings & hose. All gone :)
The problem was simple, the hose was 30 years old and had a lot of gunk in it AND the fitting beneath the sink was broken. I found that out when I tried to undo it in order to clean it out, it fell apart into 3 pieces as soon as I touched it, not even trying to unscrew it.

The drain hose, 1", also had some legacy hoses attached to it, another source of blockage. The C34 forum guys identified that extra hose as being the original fridge drain hose which has long been blocked off. I did not include that when replacing the drain hose. So now there's a nice clean run for the hose to the thru-hull.

The new unit's diameter is about 1/16" bigger than the original, but it's much better designed with a better slope 95° of the outlet.

That meant that I had to use my trusty Dremel to grind away at the sink drain hole. It only took about 5 minutes work to get it to fit in each sink. Of course, this was on a day when the AC refused to run and I did not intend to be there long enough to worry about fixing that. So I was drenched by the time it was all put back together.

Total cost was $65 for the two new drain fittings, and $25 for the new 1" hose and a tub of plumbers putty that should last me a lifetime.




We drove home and I took a long shower and drank plenty of water.

Another upgrade.

See you on the Water.

Paul





Thursday, August 17, 2017

Updating our GPS and Nav System

Garmin Update - long overdue

We have a Garmin GPSMap 741xs which came with the boat, but we have upgraded the system to a NMEA 2000 Network that includes a GMI20 Instrument and GND10 wind data input along with a Garmin Wireless Wind transducer, Garmin Depth/Speed/Water temp transducer and already had a GMR18 HD Radar. BUT - the software version was that from 2014 - Time for an update.





Here's the process that we followed:
  • Downloaded the Update from Garmin to our PC (We had to login to our Garmin.com account to get this)
  • Insert a FAT32 Formatted 4GB Micro SD Chip in the card reader of our PC
  • Run the program from the folder where the update was saved
  • The program requests the Chip ID (just pick it from the list) and then it installs the update software and data into the chip.
  • On the Boat, power up the GPS, Radar, AIS, NMEA 2000 network (On Eximius, we just turn on the Nav Instruments Breaker and that powers up the GND10 and GMI20 as well as the NMEA 2000 Network)
  • Once the GPS is running, then insert the Chip into the GPS card slot.
  • The GPS recognized the Chip and offered the option to Update the System (which in our case was from 3.80 to 6.6 - as I said, Long overdue)
  • Once we confirmed the option, and the note that we should not power down anything until the update was complete - The update began.
  • The program on the Chip updated the GPS, Radar, GND10 and the GMI20, it seems there was no update for the AIS. The whole process took about 10 minutes after which the GPS shutdown and rebooted.
  • Once rebooted, we removed the Chip - All done!
What we got in the update:
A whole bunch of features that are really cool.
  • Windward Route To Laylines - these are really useful when you know the location of a destination. It displays the Laylines on the GPS Map so that we can steer towards them for optimal speed to a windward mark. They are real time dynamic, so they change as the wind changes, very cool. But you do have to know where the mark is located or at least have a pretty good idea so that it can be entered as a way point.
  • Boundary Markers - At least, we know they are part of the upgrade but we did not get to test them out yet, that will be the next navigation how to. But they are really useful. The concept is that we can mark out an area(s) on the chart and then set our preference of either Stay within or Stay outside. eg. We could mark an area around the tip of a peninsular that had a shallow area that we wanted to avoid. Then we would create a Boundary around that area and take the option to stay outside (eg. alert if entering). Alternately, we could create a boundary and set the option to stay within (eg. alert if leaving) 
  • There were several other minor updates, they just improve the reliability of the system. 

So now we have a bunch more techy stuff to play with on our next trip. Peggy loves this stuff - and you know the old saying - Happy Wife = Happy Life 😁

See you on the water.

Paul

Saturday, August 12, 2017

Turned back

Nearly got to sail last weekend

Having completed the re-bedding of the 6 Chain Plates, which required slackening the 4 Lower and 2 Upper Shroud Turnbuckles, I needed to tune the rigging. So we made a last minute decision to take the boat out on Sunday, staying overnight Sunday & Monday and return to the dock Tuesday Morning.

On the back side, we had setup for divers to come and clean the bottom but didn't have an actual date for that, we decided we would call them Monday morning and head back early if their plan was to do the boat that day.

Sunday morning we did our routine of getting everything together for a couple of days away on the boat. We had our list, Meals, Drinks, Meds, Clothing, Bedding and Fuel for the Genny as it was going to be hot that weekend.

Arriving at the boat around 10am was fine, we had to leave by 11am in order to have deep water in the canal as the tide was going out. We quickly loaded the boat, stored the food in the Fridge/Freezer, eased the lines, tested the Engine and cast off in time.

It was an easy passage down the New River, Engine ran well, Bridges opened quickly, no snags. But as we passed the Fort Lauderdale Marina, I noticed that the wind had picked up a lot. So much for the 8 to 10 knots forecast, we were seeing 20+ knots! So I changed our plan to adjust the rigging under sail on the Ocean and decided to do the initial adjustment of the rigging just the other side of 17th Street Causeway Bridge, so we turned at the West Nun Buoy so that the wind was over the Port side and 1st adjustment made. Then we turned back to the Nun Buoy and, with the wind over the Stbd side, made 2nd adjustment. Then the Police boat headed out way! Oh Oh! We were in the Security Zone, so they politely asked to move back to the Intra Coastal and to check out Charts. Local knowledge just improved.


The wind was still in the high teens and we just didn't feel it was worth going out, so we headed back toward Lake Sylvia, we could sail the following morning if the weather improved. Picking an anchoring spot on the lake, we quickly set the anchor and opened up the boat to allow the breeze to cool it down, it was in the high 90s °F. I set the anchor alarm and the new Snubber that I made a couple of months ago, securing it to the anchor line with a rolling hitch. Worked like a charm.

Once we were secure, it was time to chill. Bottle of wine, crackers & cheese, setup some music in the cockpit, life is good.

During the afternoon, several more boats arrived and at one point there were 21 boats anchored on the lake. Kids were having a ball trying to ski around the lake behind jet skis, there was more than one boat having a barbecue and several boats seemed to be empty. We all swung around our anchors as the tidal flow changed. It's quite usual on Lake Sylvia for boats just 100' apart to experience current flow in opposite directions, so the boats around the lake were pointing this way and that, seemingly at random. 

Heavy clouds rolled in later in the afternoon, several of the power boats pulled their anchor and left, we just closed the ports, took the cockpit cushions below and put up the dodger screen. It didn't rain much.

Dinner was to be Ravioli and Veggies, but the Veggies didn't make it, they must still be in the Freezer at home. Not a biggy, cut up some tomatoes and drench them in olive oil, add some Blue Cheese Dressing and dinner fit for a king. Note to self, we really should check off the items on the list.

Chatting in the cockpit after dinner, Peggy realized that the Veggies were not the only thing left at home, the bedding were never packed! Not a biggy, we keep several blankets on the boat and had spare pillow cases. So I setup the Generator and got the Air Conditioning running. With the boat closed up due to the potential rain, the AC made it bearable below. We left it running and got turned in. Weather forecast was looking good for Monday, great, we could get out for a sail.

It rained several times overnight and we try not to run the AC during the rain as we cover the Generator, so neither of us got much sleep. During breakfast we decided to head home as soon as the tide and bridges allow. That meant getting to the first bridge soon after 9am, after the morning rush hour bridge closing. 

Taking the Snubber off took a while longer than our normal routine of just pulling the anchor, but lesson learned, I'll make a Dynema Loop that I can use to tie a Prussic knot to secure the Snubber to the Anchor Chain. We easily motored to the 3rd Avenue Bridge around 9:30am and called Andrews Avenue Bridge to request an opening. We had to hang around a couple of minutes as there were pedestrians on the bridge delaying the opening but we handled that easily, staying East of the outflow just in case - good decision, they opened about 200' ahead of us. Andrews opened and we moved over the North side the river because the Bridge Span hinges on the South side and it does not open fully vertical. As we approached the bridge, the Tender called to advise that he had heard the FEC railroad bridge was about to go down, but we might make it if we put the peddle down. We did and passed the FEC bridge which closed about a minute after we passed and called them that we were clear.

The FEC bridge is our biggest concern in transiting the New River. If it was closed for a lengthy period while a freight train slowly passed, that could cause us to miss our tide chance which could mean not being able to get to the slip for an additional 6 hours. At present there is no published schedule for the bridge closures, but there is supposed to be an App coming out that will advise of the schedule - perhaps next year!

Back at the dock, we unloaded the boat quickly and headed home, arriving about noon. Showered and Pizza put in the oven, I checked my email. Eximius was #4 on the divers schedule that day! Oh Oh, better head back down to the boat. Bedding in a bag I headed down about 13:00 to wait their arrival,

I never get bored being on the boat, there's always something to do. So while waiting for the divers , I replaced the small solar lamp above the Bimini and repaired the Speaker wiring that had broken when I was doing the chain plate work. Then I read a copy of the Mainsheet Magazine that we had on board, especially the article about how another C34 owner had modified their dodger to increase the height, which is one of the things Peggy has asked me about. I raised the Mainsail in order to measure the height of the boom with the sail fully deployed - It's 6' - as per the instructions I gave the sail maker when we had new sails made last year. Then I sent a couple of emails to the divers letting them know I was there and wondering what time they might arrive. Turns out they had arrived shortly after we left the boat to go home! I thought the hull waterline was not looking pretty good - Duh!


Stowing the Mainsail, checking all the lines, valves, and switches, I left the boat and headed home. 

Sometimes, things go according to plan, and other time serendipity steps in.

See you on the water.